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On Tue, 29 Oct 2013 15:18:38 -0400, "Flying Pig"
wrote: significant refrigeration failure item to Dick Kollmann for dissection, and so on. === I once talked to Dick K regarding some refrigeration advice for our trawler. I was contemplating the installation of two Adler-Barbour Cold Machines, one for each of our built in fridges. He didn't think the A-Bs would be suitable for tropical cruising but three years in Florida later, including two 6 month cruises to the Carib, they are still working fine. I believe they use Danfoss BD-50 compressors. Both units were self installed and I carry everything I need to service them in case we get stuck somewhere. Having two independant units gives us a fair amount of redundancy however. |
#2
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"Wayne.B" wrote in message
... On Tue, 29 Oct 2013 15:18:38 -0400, "Flying Pig" wrote: significant refrigeration failure item to Dick Kollmann for dissection, and so on. === I once talked to Dick K regarding some refrigeration advice for our trawler. I was contemplating the installation of two Adler-Barbour Cold Machines, one for each of our built in fridges. He didn't think the A-Bs would be suitable for tropical cruising but three years in Florida later, including two 6 month cruises to the Carib, they are still working fine. I believe they use Danfoss BD-50 compressors. Both units were self installed and I carry everything I need to service them in case we get stuck somewhere. Having two independant units gives us a fair amount of redundancy however. Those are good units. Even the air-cooled version works well in the tropics. The key to success seems to be placing the compressor in a spot that doesn't get hot (don't put it near the engine space) and can be set up so the cooler air goes in through the little radiator and the hot air blows out elsewhere. My Adler Barbour started acting up (cycling off and on with the compressor running for five to ten seconds to a minute and then cycling off (as evidenced by the amp draw - the fan kept going). Turns out there are about six spade connectors going into the control panel. Some of these had gradually loosened up and were making poor connections. I pulled them loose (the female side is on the wire, crimped the female side tighter, applied some dielectric paste and slid them home. It's worked flawlessly since. I've experimented with the amount of R-134a and found that a suction pressure of 7-9 psi results in the best refrigeration vs. amp draw. I've fitted the suction side with a NAPA injection port for auto A/C that fits the standard can of R-134a injection hardware and gauges. -- Sir Gregory |
#3
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"Wayne.B" wrote in message
... On Tue, 29 Oct 2013 15:18:38 -0400, "Flying Pig" wrote: significant refrigeration failure item to Dick Kollmann for dissection, and so on. === I once talked to Dick K regarding some refrigeration advice for our trawler. I was contemplating the installation of two Adler-Barbour Cold Machines, one for each of our built in fridges. He didn't think the A-Bs would be suitable for tropical cruising but three years in Florida later, including two 6 month cruises to the Carib, they are still working fine. I believe they use Danfoss BD-50 compressors. Both units were self installed and I carry everything I need to service them in case we get stuck somewhere. Having two independant units gives us a fair amount of redundancy however. The replacement unit will be a Sea Frost water-enabled (nothing there yet, but available to hook into the next time we're in the yard) DB50 Air/Water cooled, with smart controller and thermostat (incorporating a Carel, from the looks of it) and two 15x19 evaporator plates. I have every confidence that this will be more than adequate to the task, especially as I'll vent outside air to the air cooler incoming fan (venting already in place, ironically, from a blower we used to use on the alternator before we figured out what was causing the horrible failure rate), which will blow it over the compressor to cool it, too. If I get the urge, I can add water cooling to it, and PERHAPS the added amp might be recovered in shorter run times. However, as I'll have a smart controller, and the pump will run, regardless, if it's used, running at low speed doesn't get much of a boost in efficiency. If it works in the tropics, I'll do a nevermind... L8R, y'all Skip, with family coming tomorrow and weekend -- Morgan 461 #2 SV Flying Pig KI4MPC See our galleries at www.justpickone.org/skip/gallery ! Follow us at http://groups.yahoo.com/group/TheFlyingPigLog and/or http://groups.google.com/group/flyingpiglog When a man comes to like a sea life, he is not fit to live on land. - Dr. Samuel Johnson |
#4
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On Thu, 31 Oct 2013 16:37:37 -0400, "Flying Pig"
wrote: from a blower we used to use on the alternator before we figured out what was causing the horrible failure rate ==== I have my own tales of alternator failures, finally resolved. Don't think I've heard about yours. Our failures were caused by the *very* large house bank (8 HD golf cart batts in series-parallel), which appeared to the alternator more or less as a dead short when they were in need of a serious recharge. The solution was a controlled series resistance consisting of 10 ft of #4 wire which was just enough to limit the current inrush to acceptable levels. |
#5
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"Wayne.B" wrote in message
... On Thu, 31 Oct 2013 16:37:37 -0400, "Flying Pig" wrote: from a blower we used to use on the alternator before we figured out what was causing the horrible failure rate ==== I have my own tales of alternator failures, finally resolved. Don't think I've heard about yours. Our failures were caused by the *very* large house bank (8 HD golf cart batts in series-parallel), which appeared to the alternator more or less as a dead short when they were in need of a serious recharge. The solution was a controlled series resistance consisting of 10 ft of #4 wire which was just enough to limit the current inrush to acceptable levels. Mine was a case of a 1/2" pulley on the alternator when the design was for 3/8, and not using a corrugated belt which would flex at high speeds, dissipating heat. The mount-twiddling was a mere benefit, rather than just solution Went from 10 to 200 hour belt changes, and the 10s were usually catastrophic (breakage)... I've recently shortened the belt to get more mileage out of the adjustment, as the belts I took off weren't worn out, just stretched out. However, I only have 880AH, and my alternator isn't doing the work; it's solar and wind, plus occasional application of a Honda eu2000i to the charger. Good workaround! L8R Skip -- Morgan 461 #2 SV Flying Pig KI4MPC See our galleries at www.justpickone.org/skip/gallery ! Follow us at http://groups.yahoo.com/group/TheFlyingPigLog and/or http://groups.google.com/group/flyingpiglog When a man comes to like a sea life, he is not fit to live on land. - Dr. Samuel Johnson |
#6
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On Fri, 1 Nov 2013 11:30:16 -0400, "Flying Pig"
wrote: "Wayne.B" wrote in message .. . On Thu, 31 Oct 2013 16:37:37 -0400, "Flying Pig" wrote: from a blower we used to use on the alternator before we figured out what was causing the horrible failure rate ==== I have my own tales of alternator failures, finally resolved. Don't think I've heard about yours. Our failures were caused by the *very* large house bank (8 HD golf cart batts in series-parallel), which appeared to the alternator more or less as a dead short when they were in need of a serious recharge. The solution was a controlled series resistance consisting of 10 ft of #4 wire which was just enough to limit the current inrush to acceptable levels. Mine was a case of a 1/2" pulley on the alternator when the design was for 3/8, and not using a corrugated belt which would flex at high speeds, dissipating heat. The mount-twiddling was a mere benefit, rather than just solution Went from 10 to 200 hour belt changes, and the 10s were usually catastrophic (breakage)... I've recently shortened the belt to get more mileage out of the adjustment, as the belts I took off weren't worn out, just stretched out. However, I only have 880AH, and my alternator isn't doing the work; it's solar and wind, plus occasional application of a Honda eu2000i to the charger. Good workaround! === I've had good luck with Gates "Green Stripe" belts, available at NAPA auto parts. 200 hours is still not all that good. There must still be another issue somewhere. Having experienced any number of belt and alternator failure modes, I can tell you that a nice clean belt break is preferable to a whining, squealing burn up which is throwing off black rubber bits and smoke in the engine compartment. Our *big* alternator is now a 320 amp Leece-Neville fire truck unit driven by three belts. It has over 500 hours so far with no belt changes or signs of premature wear. Even with the current limiting resistor, the alternator causes the DD 6-71 diesel to audibly grunt for a split second when I switch in the house bank. |
#7
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"Wayne.B" wrote in message
... I've had good luck with Gates "Green Stripe" belts, available at NAPA auto parts. 200 hours is still not all that good. There must still be another issue somewhere. Having experienced any number of belt and alternator failure modes, I can tell you that a nice clean belt break is preferable to a whining, squealing burn up which is throwing off black rubber bits and smoke in the engine compartment. Our *big* alternator is now a 320 amp Leece-Neville fire truck unit driven by three belts. It has over 500 hours so far with no belt changes or signs of premature wear. Even with the current limiting resistor, the alternator causes the DD 6-71 diesel to audibly grunt for a split second when I switch in the house bank. Since 200 hours represents a couple of years or so, I'm not terribly worried :{)) Our belts are Gates, too, but from NAPA and wherever we can find it; they're toothed/cogged/scalloped on the inside, and heat, ever since, has not been an issue. But we DO have belt dust, a bit. Never had a squealer, though; our alternator's only 70A and as far as I can tell, it's never challenged the belt, particularly. In the cases where we have to motor, it will fill the bank from wherever we've gotten it down to - usually not less/more, depending on how you count, than 70%, but otherwise, it's loafing. Our solar and wind do all the heavy lifting... L8R Skip -- Morgan 461 #2 SV Flying Pig KI4MPC See our galleries at www.justpickone.org/skip/gallery ! Follow us at http://groups.yahoo.com/group/TheFlyingPigLog and/or http://groups.google.com/group/flyingpiglog When a man comes to like a sea life, he is not fit to live on land. - Dr. Samuel Johnson |
#8
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![]() "Wayne.B" wrote: Our *big* alternator is now a 320 amp Leece-Neville fire truck unit driven by three belts. It has over 500 hours so far with no belt changes or signs of premature wear. Even with the current limiting resistor, the alternator causes the DD 6-71 diesel to audibly grunt for a split second when I switch in the house bank. ----------------------------------------------------- There was a time in my life when I was a Leece-Neville design engineer. Back in those days the large alternators (200+ Amp) designed for the bus fleets had the AC terminals brought out to the case. Common practice was to grab a couple of AC terminals and install a single phase, half wave bridge across the AC which was then connected to a DC relay with the contacts of this relay wired into the field circuit. SFWIW, field current was limited to 5 amps back then. When the engine was starting, the field relay was open which basically eliminated any alternator belt loading on the engine. There is enough residual magnetism in the rotor & stator that when the engine has started and up to speed, sufficient voltage is generated to excite the relay and start charging the system. ------------------------------------------------------- "Flying Pig" wrote: But we DO have belt dust, a bit. Never had a squealer, though; our alternator's only 70A and as far as I can tell, it's never challenged the belt, particularly. ---------------------------------------------------------- You have a problem. Sooner or later it is going to bite you. The better but not necessarily the easiest solution is to move to a dual belt system. Since the alternator is not your primary recharging device, you might consider increasing the alternator sheave diameter and staying with one belt. You WILL reduce the output, but by how much can only be determined from an output curve. Lew |
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