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I must have checked the float level 10 times before I put it back
together. Of course I could be measuring it wrong however. On my rebuild kit it had a note that said that with four cylinder engines experiencing rough idle and flooding that it may be necessary to change to a spring loaded needle. So I changed it from the original solid needle to the spring needle and then readjusted the float level. Could this be causing the problem? Also you mentioned that I could have put in the power valve wrong. What could have gone wrong with it? I just put the gasket on and screwed it in. Was there something else I should have done? Thanks, James. |
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