Home |
Search |
Today's Posts |
#8
![]() |
|||
|
|||
![]()
OK, the head is done,( $250.00 worth) and the machinist said that the
seats were pretty beat up which would recess, and through the valves out of adjustment.... ie. the valves would lose there lash against the rockers, and would be forced to stay open even just a couple thousanth's or so and not close tightly. So it got a pressure test, plane job, new valves and seats, seals springs tested. New head bolts and gasket set. He said that the head was slightly warped in between the 2 and 3 cyl. and said that sometime in it's past life it boate engine was probably over heated. Now I did notice that when I went to service the engine the pump/alternator belt was loose and you could turn the water pump easily by hand. hmmmm. He said the carb should be richened up slightly and running the timing to spec should be fine. but seeing it's converted to Petronix electronic ignition, it should be re-timed. Once back together, I'm going to do my best to get regular fossil fuel (no gasahol) and take it from there. Tim |
Thread Tools | Search this Thread |
Display Modes | |
|
|
![]() |
||||
Thread | Forum | |||
(On topic) Mounted and Exhausted- heater report installment | General | |||
Exhaust conversion to thru-hull | General | |||
Exhaust conversion to thru-hull | Boat Building | |||
Exhaust question on inboard 1958 Chris Craft | General | |||
Exhaust question on inboard 1958 Chris Craft | Boat Building |